Date: Fri, 27 Jan 2006 02:25:21 -0600 (CST) Subject: SLA battery and new steering motor X-UID: 129 Content-Type: IMAGE/JPEG; name="img2573.jpg" Content-Type: IMAGE/JPEG; name="img2575.jpg" For $20, I found a 12 volt 4.2 amp-hour SLA (sealed lead acid) battery as a Christmas toy leftover. That includes a slow charger. This will run the digital side for at least two hours assuming the specifications are correct. Weight is around three pounds which is acceptable. It's a little tall but otherwise fits under the electronics box with the existing mount. The community that closely parallels what I'm doing are amateur radio operators. They typically have a basic knowledge of electronics and are often concerned with adapting existing COTS (common off the shelf) technology to mobile and portable use in the field. This involves problems that the electronics hobbyist is unlikely to encounter. Specifically, I found a clear explanation of why my homemade battery packs didn't work. Others have tried this with typically poor results. The battery contacts and thin gauge steel wires in the typical plastic battery holder introduce too much resistance. In my case, there was so much resistance that the wiring inside the pack was becoming very hot. This explains why the voltage would drop very quickly. The hot wires had greater resistance, which increased power dissipation, generating even more heat, etc. Eventually, the resistance was so high that voltage dipped below the cutoff for the DC-DC power supplies on the computer boards. I have some industrial style solder tab battery holders that probably will work. They're still not as efficient as spot welded commercial packs. But I have lots of NiMH batteries and these battery holders on hand so will probably make a bipolar pack (-6 volt, gnd, +6 volt) for the steering motor and cooling fan. However, right now the pack I have does seem to work so I'm going with it for Sunday. This time, I'm trying to transfer lateral loads to the screwdriver body. I think that hanging the other screwdriver off the shaft causes the gearbox to seize up. So I found a 7/16" ball bearing (the OD of the shaft is .431). By happenstance, it fits perfectly inside a 1 1/4" compression coupling. It's like it was made for it. Mating the coupling to the screwdriver body was more problematic. I had to shorten it by sawing off one end and then facing it off in the lathe. It's almost too big to fit in the chuck. Then it was degreased and epoxied to the end of the screwdriver with JB Weld. This steel epoxy has one noteable property that makes it very useful. It doesn't run like most two part epoxies do. The bearing end of the compression coupling screws off. So tomorrow I'll remove it and pour some more epoxy between the coupling and the screwdriver. I don't know if this will hold up as in my experience epoxies have a difficult time bonding to many plastics. So I'm on schedule. The task list for this evening. 1. charge the NiMH drill battery packs for Sat testing and Sun field trial 2. reinforce and reposition the battery mount for the SLA battery (shift it down with rubber washers and reinforce with aluminum bar) 3. mount SLA battery with industrial velcro (have to degrease surfaces first) 4. solder wires into the new cordless screwdriver 5. mount new screwdriver in place of the old one (may defer until Sat depending on additional epoxy cure) 6. check/modify electronics box wiring - no shorts or loose connections 7. close electronics box and mount on robot 8. basic function test of electronics, as much as fits in available time Saturday will be testing and adjustment. For Sunday, I'll use WiFi, ssh into the onboard computers, and run the robot with shell scripts. It'll perform a fixed sequence using what I've got now, nothing really new. A loose end I've almost forgotten - the webcams. These must still be mounted. I'll have to fit in Friday or Saturday sometime.